harold wrote:Your air scew adjustment is about where it should be at 6 turns, but you should have noticed a reduction in the popping, as well as more snap off of idle. The carbs are quite hard to get off, as they hit the frame and oil lines when you move them back to get out of the intake boots.
One thing you can do easily to see if there is a float problem, is remove the drain bolt on the right side carb that doesn't have the float bowl. You can get to it without having to remove anything. Gas should flow out, which you could catch in a clear jar to see if there is anything floating around in there. If it doesn't, then you are only running on one carb, and you will have to take them off.
Your lights look pretty good for the price. I would like to replace mine too, as it doesn't do a lot. What were you saying about a ballast? Does this light not work out of the box?
Thanks for the info. I'm going to run this tank out as far as I dare and see how it does. This is my 2nd tank of seafoam spiked gas. Then I will drain that and see what happens. It did not stop the popping. I'm betting the carb is super nasty.
The light itself would work out of the box, but I would want to convert it to an HID high voltage ballast and lighting system. It takes a few seconds to warm up, but it puts out a ton of light for the heat it makes, and the energy it uses. A good 55w ballast/light will absolutely wreck the output of a similar halogen bulb.
That with 2 LED floods as a highbeam/fog type light and I think I'll be set!